Update: Race day went ok... With the lack of testing time, I just went on Sunday for the "Grudge Racing". I ran a few times down the 660ft track. It ran ok, but wasn't pulling full RPM after the first 100ft or so. I also had an issue with the chain slipping which cut my day short.
Since then, I was able to fix the slipping chain with a stronger spring and new chain. I also fixed the dropping RPM with a different secondary spring. I've got it dialed in really close but I am not happy with the results. I have my modified 81 Invader 440 performing the same or better on pump gas. So...it's back to the drawing board. I have sent some 4/6 cylinders and Liquifire heads to my engine builder in Canada. The ports will be welded and reshaped, the heads will be shaved and reshaped as well. I am also replacing the pipes. I have started to modify some 4/6 LTD pipes to specs given to me by the engine builder. Tuning it to run 9200 and with open stingers, it'll be fast and loud!